OK...
Just a quick post from me as i WILL NOT get pulled into any forum flame wars.
Facts time.
I mapped your car roughly 2 months ago (may have been closer) and your clutch was slipping, your car was boosting too high as the actuator is set to 1.2bar min. I told you to get a clutch fitted and that the car was not safe to drive hard until the map was finished. I even went to the length of removing your boost controller to give as much safety as i could to make sure the car came back in one peice. The first thing you told me when you arrived was that the car had been boosting to 1.2bar and you told Matt in the office that whilst your mate had been driving the car the car had hit 1.7bar WTF!
A few points, firstly on removing your spark plugs you have standard heat range spark plugs fitted. Not even 7's,
BKUR6 When you brought your car up to me last time i asked you clearly if everything was specced to support the power wanted, you said the only weak link was the clutch which was true and it slipped.
You told me that you had an oil change on friday, after commenting on how black the oil was a few times you said that the oil had been topped up. When i dipped the oil it was .9litres low and only just showing on the dipstick, this was after being filled on friday.
As agreed by everyone in the dyno cell there is/was about 100ml of oil on the floor, ironically the oil on the centre beam was from a golf turbo that split an oil pipe on the dyno on sat. It isnt anywhere near where your breather is.
Lets go with all the oil in the whole cell is from your car, 100ml not .9litres.... In fact, why did your car 'need a refill' on friday...
When you first came in you told me the rocker cover was leaking badly, i had spotted a small 3mm spec of oil on the SIP on the turbo but this was below the rocker cover leak.
I set up my equipment on the dyno, fitted your boost controller again and got started, as usual practise i pull timing so i can work back up again.
I did 3 light throttle drives up to 3500 to check fuelling was close low down, happy with that i reset the boost controller and started the first power run. As boost came up i came off the throttle as i was not happy with the smoke from the exhaust. I brought the car back onto light throttle and there was no smoke but i was not happy to continue. I checked under the bonnet and there was oil from the breather, i then asked if you was happy for me to do a compression test to ses if comp was down. On pulling the plugs i noticed they were the wrong grade for your tune and that plug number one had signs of det on it, there was no det whilt i had the car on the dyno as i had my det cans on and the timing was pulled back.
After a bit of blaming from you i got my own camera out to take some pictures, on closer inspection the oil filter is leaking badly the rocker cover is pissing out. The underneath of the car is soaked in oil (all photographed), when oil leaks on the dyno, the fan is so strong it blows the oil across the floor as will show in a picture you took. Not soak the underneath like tha car has been waxoiled, and certainly not on the other side of the car under the oil filter ;).
You told me that the car had never dropped a drop of oil on your drive, yet the oil filter is soaked/rocker cover pissing out/ sump leaking/turbo oil leak (confirmed by your mechanic)? Come off it!
Your car is running exactly the same as it came in, not missing a beat. It starts and runs fine but as i told you yesterday i am not happy with the breathing. there is no smoke from the exhaust on idle or light throttle, i am not happy to bring the car on boost as there is a problem there as we have found.
A representative from our dyno was updating our software to the new release on a new operating system (down form sunny scotland

) the extrapolation for drive losses was out if i did not complete the run, the dive losses are calculated over a % of the run. As i came off the throttle due to the smoke the run was only to 5000rpm which gave an incorrect power figure. I cleared the run as i always do, this is as i will never give out an incorrect power figure FULL STOP.
The sofware has been configured now and all is fine.
You paid for an hours mapping which would have included a graph normally, however i was not happy to run your car again so you do not have power graph.
If anything everyone reading this can perhaps learn something, if your car is not built by us you need to make sure everything is in place to support the power you want.
If you tuner is happy to bolt on a turbo that is capable of 400+hp try and make sure you
a: have the spark plugs to go with it
b: if you have abnormal oil usuage find out why
c: if you are told the map is not complete and to take it easy until its finished due to slipping clutch, dont let your mate hit 1.7bar
d:if you boost is set to 1.2bar std and i ask you to get it dropped, i'm only trying to advise you what i think is best.
e:understand i am always on the end of the phone for advice, even if your own tuner doesnt want to make the call give me a shout.
This time i will publically state this so there is no confusion! Your car needs the boost dropping, you need the right grade of plugs, you need to sort the oil leaks out and you need to not drive your car hard like i told you!
When i told you this, you stated to me that 'you took too long to get me back in'.
We are flat out at the moment and i apologise for not getting you back in sooner BUT... you knew the score, dont drive the car hard!!!!!!!!
I wont get back on here as i have stated the facts, your car is here ready for collection as you brought it.
You told us yesterday that you are coming today with your mechanic. We are looking forward to talking to him.
Just to make sure all is clear as i havent read through the whole thread, roger from power fiat did not build this engine and AFAIK only topped the oil up. No question at all about his work.
Last but not least, is there a longest post award

Cheers
Rob